Home made Tube
Workshop Roadster Projects Photography
We always look to do things
different at time or to improve on what we have. One item I
have long thought of changing is the roll bar on the car. It
slopes in towards the top, is made from Scaffolding and really
does not go over my helmet when driving so any chance of flip and
I think my head would get squashed.
So changing it for a slightly taller one and try to meet MSA Blue
book regulations should be better.
The Blue book gives minimum sizes for tube of 45 mm x 2.5 mm wall
or 50 mm x 2.0 mm wall. It requires a diagonal on the main
loop and two back-stays, but mainly taller then when wearing a
helmet and squarer in general shape.
I visited a place that could make one for me and was roughly quoted
£300 painted. I could not easily justify this so looked
at making my own bending device for the 45 mm x 2.5 mm wall tube and
basically making my own roll bar.
27th December 2012
So I set about going through my metal pieces in the workshop and
started to fabricate my own bender.
Looked around my metal pile and found some
10mm plate and some old rusting metal around 18mm thick, formed a
sandwich with 3 x 10mm pieces approx 200mm square and then 2 x
18mm pieces across diagonally. Drilled for 6 10mm bolts and one
big hole at 1" diameter for the pivot point.
Lots of work on the band saw to rough cut and then down to the job
of rounding the piece to a 100 degree quadrant. I completely
trashed a dividing table, just was not big enough for the job as I
ended up breaking the gears, so had to improvise.
This was my answer.
I had to take breaks from the job to allow the feelings to settle
back in my arms and fingers. And to think I should know better
being H&S trained.
The next step is to rough cut the groove in the blank before
finish cutting. At this rate in a week or so.
4th January 2013
I have sort of finished machining the die,
may need a bit of emery work, but will do for a starter.
Will have to do the frame next and see how bits go together!
12th January 2013
I got bored, it's not finished yet, but I
had to try and see if it would work, well you would wouldn’t
you? Built up the frame and cut a few guides out of
aluminium block, placed things together and had a bend!
The guides are just sat on a base plate as could possibly be
seen. So started to
bend the tube.
I ended up over the 90 degrees with spring back so need to work
that out. There is a slight
kink starting on the inner edge of the bend, not sure if you can
see this in the pictures. I think this could be down
to the tube guide is not under the die centre line. It needs to
have shoulders on the front face to allow it to sit below the die,
so at present is 1&1/2 " behind the line, when I have done
that I should be able to check for clearances and make sure the
guide is as close to the die as possible.
Oval-ation is less then 90% so happy with that.
13th January 2013
The unit is now all but finished, changes to
the guide height by lifting it up by 4mm kept the tube tight
against the die on the inside bend. Decided to do a proper test
bend on a new piece of tube so I marked out rings at 20mm spacing.
Stuck it in the rig with the first mark at the end of the half
Took it out and stuck against a plate to take picture. No kinks at
all nice and smooth so very pleased with the result.
Again checked the squash and got 41.25 mm so still happy with
Basic measurements are 70mm from first mark
to start of bend and bend radius is 6.2 inches so I have 0.2 inch
(5 mm) of spring when I take the tension off, the die is 6 inch
radius. I think I will clean and paint the unit before
it goes rusty with the cold weather.
3rd February 2013
The frame is painted and I just had to go at the main loop, it
worked out OK, so now have to just get on with it.
31st March 2013
long time and no update so about time I caught up. I had to
get more tube, with all the setting up and test pieces I ran out of
the stuff. But anyhow more lengths bought, some plates for the
main loop mounts purchased and time on the milling machine with a 45
mm hole saw and I have the following:-
I have also been spending time welding in some square tube and
plates at the rear of the car to mount the back stays against.
this was a nervous affair with the petrol tank below it, so drained
the tank, sealed the filler, covered with sheets of aluminium and
steel to stop moulton metal from hitting it etc. and I have got away
with it. There is some damage to the rear paintwork that will
need to be repaired and some filling to make the area smooth where I
have cut sections of the aluminium top away, but it should look OK
when finished. I am taking the rollbar to be welded, rather
then do it myself, it needs to be correct first time.
2nd April 2013
Back from the welders and all fastened together:
I will get it painted and bolted down over the
next few days. A new boot lid is now required.
© A Hodgson